Battleship
Radio Project
Photos
Part 1
This
past July (2000), while I was setting up to work the Museum Of old ships from our
club station of many years, I was approached by Kim Sincox who is Museum
Service Director on the ship. Kim wanted us to move from our location
behind the bridge to another location on ship. The ship wanted to open the
room that we used for years as a display.
The
following week our club president Frank - N2EMR,went over and met with
representatives from the ship. From that meeting came a new partnership
between the Azalea Coast ARC and the battleship. We would move from our
location on the bridge to the location of our choice. The ship would also
help us by providing their electrician, Terry Kuhn, to work with us one
morning a week. The ship asked our help with some of their projects which
included the " Charlie the Alligator Party " (Kids Day on the
Battleship) and help with restoring some of the old radio equipment.
The
next 6 weeks a large group of the clubs hams helped to get 3 antennas up
and working. Our new radio room was to be the original ships radio central
room , which is located below the water line on deck 4. We have a 3
element Yagi for 2 meters, an original ships vertical for 40 & 15
meters and another ships vertical for 20 & 10 meters. Thanks to Terry,
the ship's electrician, we located the original ship coax and was able to
splice into them to get the coax from the super structure to the radio
room.
We
learned a lot about the ship while working on the antennas and the
problems we had with them. Radio central is located about midway ship on
deck 4 and the transmitting room is located about midway ship deck 3. To
make things flexible the ship has coax patch panels so that they can put
any antenna on any transmitter via the patch panel. So far we have found 3
patch fields.
The
first problem we had with our antennas was that they just didn't work at
all. We imagined a lot of things like the coax we spliced into were bad or
the impedance of the lines was way off. We have no idea what the impedance
of the original coax is. The problem turned out to be that when we patched
the coax, we patched them in the wrong jacks. We had continuity on the
lines but when we took a ohm meter reading we found that we had a high
reading, 600 ohms on each line. The point that we patched at carried a 600
ohm terminating resistor. After we move the patch to the correct jack
things worked a lot better. Another problem was we had to clean the patch
field cords and plugs. We had a lot of trouble getting connections through
60 years of neglect.
In
radio central the original jacks are not like anything we use today. The
ship wanted to keep the equipment in it's original condition so we cut one
of the patch cords in the middle to plug into the jack and we put a PL-259
on the other end to mate to our radio's. When I cut that coax I was
astounded to see how it was constructed. The dielectric was solid Baklite
about 1 1/2 inches long and put on the center conductor like beads.
Thanks
to a lot of hardworking club members we now have a good radio room on the
battleship. I am sure some other problems will come up but we can iron
them out.
After completing the club antenna project, the
battleship wanted us to restore one of the ships original transmitters
.The TBM7 was selected for several reasons, best reason was it had the
least damage from scavengers and it had CW and AM modes of operation. This
transmitter will tune any frequency between 2.0 MC and 18.1 MC with 500
watts out on CW and 350 watts on AM. The transmitter sits in 2 six-foot
bays; bay 1 is the modulator bay for the AM operation and bay 2 is the
transmitter. It requires 440 volts, 3 phase, which was normal ship power.
The 440 v runs a motor generator that supplies all the voltages to the
radio.
Going into the project we knew we had some challenges
to overcome. Missing equipment, missing antennas and no power.
Carl, KC8BQT, Terry, ships electrician and myself
studied the job and came up with a plan to attack this job. Scavengers at
some point had removed 2 meters from the transmitter and 2 meters from the
modulator bays. Carl started to work on getting meters and Terry started
to work on getting power to the radio. I found a job that I could do; it
required skill with a broom and a vacuum cleaner. The transmitter room had
not been cleaned well in 60 years.
I should explain at this time, we only work about 3
hours a week on this project. Normally on Tuesday mornings from 9:00am to
about noon. This is the time that the battleship has allocated their
electrician to work with us.
About a month into the project we had 2 meters
installed in the transmitter bay and we had 440 power to the power panel
in the radio room. We decided not to worry about the 2 missing meters in
the modulator for the time being. No AM operation planed any time soon.
The next step was to check all the power leads with
an ohmmeter in preparation to power up the transmitter. A lot of equipment
had been removed and some was just cut out with bare wire lying around.
All leads checked out good. We were looking forward to the next visit to
crank the motor generators. We had checked the grease in the motors -
generators and they were ready.
The following week we arrived with our voltmeters and
fire extinguishers. We were ready to power up the transmitter. The start
button was mashed to start the motor and nothing happened. Back to the
drawing board and schematics. A week went by before we found that an
interlock switch in the modulator bay was not making contact. There is
about 8 interlock switches in the 2 bays. These switches are not
complicated at all, just a piece of metal that wedges between 2 other
pieces of metal. The connection seems to be good but must have had a film
over the connection. The metal was cleaned with sandpaper and we got a
good connection. We decided to wait until our next visit to try again to
start the motor-generators.
On our next visit, with great anticipation the motor
start button was pushed. The sweatiest sound you ever heard, it cranked
and ran like a sewing machine. We were ecstatic, the tubes were lighting
after 60 years. It didnt take
long to figure out that although the motor-generator was running we had no
DC voltages. Back to that drawing board with the schematics. We could find
no reason for us not to be getting the voltages. Time to go home for this
week.
During the next week we were asking around for ideas
on our problem. Clarence, KB4AKH, came to our rescue. He came over the
next couple of weeks and cleaned the armatures and brushes and brush
holders on both of the generators. This fixed our DC problem, we had all
the voltages. Time to take another baby step forward.
On our next trip over we had current meter readings
on the master oscillator but that was all. We decided to key the
transmitter via a test key on the front panel. Nothing ! Back to the
drawings. Everything looked good. Carl reached up and tried to manually
operate the keying relay, it was frozen solid. We had to repair the relay;
a new relay was out of the question, another challenge for the team. The
next couple of weeks were spent trying to get the relay out and repaired.
The challenge was met after a lot of prayer, mediation and a few other
words.
Well moving right along now, the test key will key
the keying relay. Problem is that we still dont have any meter readings
on the next stage. Back to the drawing board! We worked on this problem
the next week and Terry found a loose resistor in the screen grid circuit
of the second stage. These resistors plug into clips in the bottom of the
bay. Hey! Hey we are getting
all the meters to read !
On our next trip I brought a power meter and a dummy
load to test with. After reading the lineup procedures we were getting 60
watts into the dummy load.
Now we dont have any idea what impedance this
transmitter is looking for. From what I understand back in the days of
this transmitter SWR had not been discovered yet. They never give it a
thought, there is nothing in the Navys book that mention SWR. There are
large tuning inductors and capacitors in the antenna tuning circuit and
you tune them until you get the reading on the finals that you want. The
transmitter has a plate on it that says that the antenna is 108 feet in
length. In other words the heavy cable coming out of the transmitter (1/2
inch in diameter) going up through the ship to a vertical antenna is all
part of the antenna. They used the same antenna to work any frequency
between 2 to 18.1 MC and no tuner. Tubes are a lot more forgiving with SWR
than transistors but this is very different.
Well, we are happy, we have power out. The next step
is to hook up a real CW key to the transmitter. The next week I wired in a
CW key through the patch field and tried it. You guessed it, it dont
work. After checking the drawings we found out that we have a bad switch
on the transmitter. This switch is a remote or local operation switch. The
back of the switch has several sets of contact on it much like a relay.
The contacts have little arms on them and several of the arms are bent
bad. This brings us up to date. We are trying to figure out how to get at
the contacts to repair them.
The Project Continues
Part 2
The
Project Continues-1 year
The
bad “Remote- Local” switch on the TBM-4 transmitter proved to be
difficult to repair. After looking over the job the entire team agreed
that the only way to get the switch out for repair was to cut all the
leads and then splice them to get them back in. The next week we started
on this repair. We cut the switch out and marked all the leads and then we
had the switch in our little hands . It took another week to get the
contacts adjusted to our satisfaction.
On
our next visit we reinstalled the switch but, to our amazement, we still
could not key the transmitter. Our first thought was we had installed the
switch incorrectly. We checked all the wiring against the drawings and
were convinced that the switch was installed correctly. After two more
weeks of troubleshooting we decided that the problem had to be in the
switch itself. We removed the switch again to check it once again and
immediately saw the problem. A contact had slipped out of place when we
put the switch back on the first try. After realigning the contacts and
installed the switch for a second time ( this was a lot
faster than the first time ) everything worked and we could key the
transmitter with a hand key.
The
next step was to be able to key the transmitter from radio central. To
accomplish this you must use a patch cord in the patch panels in order to
pick up the keying leads in Radio Central. When we checked the patch cords
we found that almost all were bad. Carl,KC8BQT took the cords home and
rebuilt them. On the next visit we checked the leads from Radio 2 to Radio
Central. All the wiring was good so we are ready for the big test. Before
we can test the transmitter from Radio Central we need some voice contact
between the two radio rooms. Clarence, KB4AKH and I worked on the existing
telephones and got the telephone in each radio room to work. Now that we
have voice contact we are ready, Terry, ships electrician, and Carl were
in Radio 2 and we are in Radio 1. Clarence had the honor of pushing the
motor start button and the motor generators in radio 2 cranked up.
Beautiful! We let the motor generator run a few minutes and then I
operated the hand key in Radio Central and Carl who was watching the
transmitter in Radio 2 immediately let us know we are keying the
transmitter.
After
almost a year of work we have a transmitter that will work. Progress is
slow but steady; we still don’t a complete antenna on our transmitter.
About 45 feet of the transmission line from the 02 level to the vertical
antenna is missing. The ship sent Terry to Norfolk and to get more
transmission line and connectors. We got lucky when the ships crew was
able to use a contractors scaffolding to remove the vertical antenna .
With the antenna on the deck we see that it needs a lot of work. The
connectors are rusted off and a lot of the bolts holding the antenna were
in bad shape. For the next 3 weeks we scraped paint and rust in order to
refurbish the antenna .Now that it is painted and put back together the
antenna is ready to go back up when ever we can get the use of some
scaffolding to put it up .Up in the air the insulator on the bottom of the
verticals don’t look to big but when it was on the deck I found that it
weighs at least 75 pounds ! It’s going to take a block and tackle and a
lot of muscle power to get the antenna assembly back on top of the
smokestack.
While
we were working on the transmitter we found outs some bad news from the
ship. The idea that we had from the beginning was to operate from Radio
Central. We have everything that we need there: antenna, keying leads and
good operating condition. The problem is that the ship requires a fire
watch in Radio 2 for insurance purposes when the transmitter is in
operation. This means that if we operate from Radio Central that someone
must sit in Radio 2 with a fire extinguisher.
To
solve this problem we plan to operate the CW Transmitter from the
transmitter room , Radio 2. To do this we need to patch a receiving
antenna to a working receiver in Radio 2. This is what we are presently
working on. Terry had received approval to work on the air handling
equipment for Radio 2 and last week he was able to start the air handler
in Radio 2. Then the fun started !That air blower had 60 years of dust,
dirt and corrosion in it and the fan blew every bit of it out those ducts,
covering everything in Radio 2 with a thick coating of grime . We spent
all day with vacuum cleaner, mops, brooms and dust rags cleaning up Radio
2. It was worth it, we now have good
air movement in radio 2.Let me tell you it’s been hot down there this
summer with no air moving what so ever!
At
the present time we are waiting to get the antenna back up on the smoke
stack and working on getting a working on getting a vintage receiver
working in radio 2. The project continues!
Jack WD4OIN
Link
to Part 3 January 2002
|